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50 Years ago today - at EVERCREECH - S and D. Mike Roach

12/6/2015

 
Hi Keith
Please find attached a short item and pictures of a railtour at Evercreech Junction, 50 years ago today.
You also have the fireman's version of the trip that day.  (On the Menu go to 'Beyond Taunton and Honiton' and then select 'S & D Bath Green park to Evercreech' - you'll find many of Ian Bunnet's stories at the end of this section).
The pictures show the train stationary, moving off, and going away.
Regards Mike Many thanks Mike.
Picture
92238 at Evercreech on the 12th June 1965. Copyright Mike Roach
Picture
Looking majestic 92238 starts to move off over the level crossing on its way towards Bournemouth. 12th June 1965
Picture
92238 gathering speed down grade towards Wincanton. 12th June 1965 Copyright Mike Roach.
A rough journey – learning the hard way     Problems with a 9f

It was June 12th 1965 I was to work a special to Bournemouth  from  Bath Green Park,  it was for  the Warwickshire  railway  society.  The engine for it was a 9f  number 92238 that was brought over to Bath and had to be "serviced" by the fitters  etc. However because it was late onto the shed  and it was a Friday  the fitters,  in their wisdom decided  a quick  once over  would be sufficient. However,  they were wrong. Come Saturday morning I came in to work it, and I had to prepare it. It was overcast and drizzling, I  had to coal and water it. I took it to the coal stage  and  back onto the boat road by the sandpit. I then  had to fill the sand boxes,  believe you me it is quite a climb to get on and off the plate with sand bucket. Taking over 30mins just to do that. Then I  had to go looking for fire irons, and then  build the fire up. I was soaked in sweat by the time I had cleaned the footplate. By then it was almost time to leave the shed.  In a rush I just had time to  run down to the cabin  make tea and get back on the engine ready to come off the shed.  We  went  to the station and backed  onto the train, we had a couple from the society  to record the journey  plus an inspector.  It was crowded on the footplate and  I  had a job to move around, then the engine started to "blow off" to stop this I started to top the boiler up.  I only did it because I  got a rollicking  about  an engine blowing off in the station.  I was only about  17 or 18 years old,   worrying  and trying to do everything right.  We left the station and at Bath Junction I  took the tablet in,  got the catcher in. However that was the start of my problems for as we started to climb  the engine started priming, we  just  about got up  to Moorfields and struggled to Devonshire tunnel. We crawled up  through  there we started to run down through  Combe Down tunnel out  over Tucking Mill viaduct to Midford. At  Midford station  we gave up the tablet.  By this time  we were a few minutes late and I was struggling to make steam which was all the harder because  of so many on the footplate. We were able to go through to  Radstock  where started the climb  to Midsomer Norton however by the time we got to "Norton" we were struggling which continued until Binegar. Here it was suggested by the inspector  we stop for a blow up, my driver -Ray Adams agreed. I  did everything I could to put  the fire right so off we went, it was all downhill to Evercreech Junction and wasn’t too bad a run.  At Evercreech Junction  I filled the tank. We set off  once more, however,  by the time we got to Cole (for Bruton) we were again struggling for steam,  the steam pressure  was just enough to keep the brakes free.   By this time I was  feeling weak and  embarrassed, I had also  been uttering expletives  and  I’m ashamed to say  I ruined their recording because of it. -  To this day  I am sorry.  I can only hope that I have been forgiven?  We struggled to Bournemouth arriving two hours late.   I think  their tour was altered because of our lateness.  We had to come back to Bath light engine.  We got back as far as Midford with  no trouble  took the  tablet and were looking forward to getting back to shed.  Just as we got to the Midford side of  Combe Down tunnel I decided to close the dampers , as I did so  we entered the tunnel and  the fire blew back into the cab Ray was behind the A.W.S  so he didn’t notice I couldn’t go anywhere  because  the tunnel was only just wide enough for  engine clearance ( If I tried hanging off the side  I would have been part of the tunnel wall!) I shouted  but I think it was luck that Ray looked up and  put the blower on harder and  kicked the fire doors closed, he also opened the regulator. The ‘blow back’ took off my eyebrows,   singed  the front of my forehead also giving me a few superficial  burns.  Back at Bath Green Park they took the engine out of service for examination.  It was found that  the steam tubes were blocked, we had  a piston problem plus a few  other problems. I got the blame for the trouble we had , they said my firing  was not right.  A few weeks later I had an inspector  Mc Carthy ride with me who said he couldn’t fault  my firing.  I didn’t get an apology for being blamed falsely. The society  gave me a couple of pictures. I have been told it was the last time a 9f went over the Somerset and Dorset. 

For more of Ian Bunnetts true stories of a Firemans Life on the Somerset and Dorset - go to 'Beyond Taunton and Honiton' and then select 'Bath Green Park to Evercreech'

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